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Jame Augustine / Carl Parsons

Australia, 1972 Escort Mk1 Cosworth, "Defuse Diabetes" Sports Sedan

Here are the cars specs
1972 Mk1 escort 1100 (originally)

Engine:
  • Normally aspirated twin cam YB cosworth
  • Argo rods
  • Cossie turbo crank
  • Burton Valves
  • Modified hydraulic buckets
  • 1X Tighe cam
  • 1X Wade cam
  • Custom mandrel extractors
  • Speed Technology throttle bodies
  • bosch 803 injectors
  • Custom Flywheel
  • Burton 3 stage dry sump
  • Autronic EFI
  • Crank triggered ignition
  • Sequential Injection
  • Custom Alloy Radiator
  • Ap twin plate clutch
  • Aeroquip braided lines and fittings
  • MSD ignition and coil
  • Cosworth leads
  • Custom Dizzy

Suspension & Brakes:

  • Adjustable Konis shocks
  • Willwood calipers Front
  • Sigma calipers Rear
  • Cart springs rear
  • Adjustable height struts front
  • Castor adjustable sway bar
  • Quick Rack

Others

  • Alloy bellhousing
  • Quaife H/D 4 speed Straight cut Close ratio race gearbox
  • Quaife alloy spool
  • Assorted diff ratios
  • 13X8 minilites
  • 230 Bridgestone slicks

The Parsons/Augustine Escort story. (www.defusediabetes.info.au)

How did Mk1 Escort #55 go from a wreckers yard in Dandenong to be travelling around the state as an under 2 litre sports sedan? Well to start the story, I had no interest in cars till after starting uni. Here another prospective university student named Karl came along with an interest in racing, but no vehicle to do so in. He was an Escort person, and I had no preference in vehicle, so after much discussion on the relative merits of Datsun 1600’s and Escorts, we acquired a 1971 Mk1 Escort 2 door to use in some sprints. We picked it up for nothing, as it has a crashed front left guard, then exchanged our skills (none) for some panel beating on our car (we cleaned the panel beaters yard of rubbish for him, in exchange for the panel beating).


The first two cars

First sprint

Following this, we purchased a 1975 Mk1 escort (late model with Mk2 type Chassis, ie has upright Mk2 style shocks, high back seats, gearbox mounts further back etc) with a 2 litre already in it for $250. It had all of the bits we needed for the conversion, including the loom, it had extractors, and a 2 inch system. The engine was an almost new reconditioned Pinto, running very well, but the body was crap. So we swapped all of the mechanical parts from the 2 litre into the other Mk1 1. We then dumped the left over 1300 engine, gearbox, body and other bits.

We took it in its first sprint using an RPM 3 point harness, and the standard low back seats. It did quite well but was probably quite unsafe. We had a great time, especially with the open diff, leaving big wheelie marks coming out of the corners of Winton Raceway.

Before the next sprint, we painted blue Cobra stipes down the length of it, put in a race seat, 13X7 Hotwires, a set of Falcon FK06C’s. We had a full alloy cage put in it, we also put in it a set of Autometer gauges, including a shift light, and recallable tacho, plus a race seat and simpson 5 point harness. We took it out in its second sprint, where at Calder Park Raceway, I promptly rolled the car after clipping the inside curb at Mt Jane. That was the end of the first car, as every panel on the car was damaged, and it was well beyond repair.


The car after it was rolled

The current car

Over the next few weeks, we searched for a new shell, and for $250, we bought another Mk1, this time a 72 model, with high back seats, but still the old chassis. This is our current car. We stripped it and had it painted, had the rear guards flared in metal, and had fibreglass twin cam flares put on the front. The roll cage was taken out of the last car, and put into the new shell. The car was sprinted for a year, with small changes over this time. It had twin 42mm Webbers put on it, Vented front rotors, Black Flash Pads, Mk2 2 litre brakes all round, including lines and cylinders. We also put in adjustable Koni shocks all round, a set of race springs in the front, a re-rated, lowered set of leafs, and had the cross member redrilled for more negative camber. We also machined the front sway bar for caster, and had a few different diff ratios locked up.

Next we started Club Car racing, and found that we required still more changes, like a laminated screen(which broke first race out), and other minor safety changes. We were, after two seasons of racing, still using the stock pinto engine, we hadn’t even taken the rocker cover off it. This went well enough for sprints, but we were a long way off the pace in club car racing with a stock engine. I started cross entering into some U/2 litre sports sedan races, and found, to our amazement, that we had many cars racing at the same level as us. It was close exciting racing, especially compared to the Club Car racing, where unless you have a turbo 13B RX7, you are not even in the hunt. The people there were so much more helpful, with other Escort guys offering us assistance with our car, including suggestions on mods, offering parts. All of this lead to the car leaving club cars and joining the U/2 Litre sports sedan series.

In the search for more power, we went and bought an already ported head, with a wade 520X cam, and group 1 valves. We also got a friend who runs an exhaust place to custom make a set of large diameter extractors for the Escort. This sounded like a good combination, but in fact, the bottom end was stuffed (no compression), so it didn’t go at all well. We also found that the valves were standard, and the porting was very inconsistent on the head that we had just purchased. So we kept the cam, and took a fresh head down to get ported (actually about 4 till we found an uncracked one). This was ported, and the group 1 valves were put in. The inlet and exhaust were match ported to the head also. This gave us about 10.75:1 compression. Cast pistons and standard rods, dowelled flywheel also went on. With all of this balanced, lightened, and put into a re-sleeved pinto block (to keep it under 2 litres). We had to use cast pistons, as we were unable to find forged pistons that were of a standard bore.


Sprints at Winton

First Club Car race

From here we put in the adjustable ride height spring platform on the front struts. On the fueling side we installed a baffled sump, and twin 50mm Webbers with a Holley blue fuel pump, regulator, and 3/8 fuel lines. Other changes included a Speed Technology rev limiter and shift light, a new twin core close fin radiator, a disc brake rear end, a pedal box, and put new brake lines throughout the car. This all sounded good, but we struggled to get any balance out of the brakes. We had the engine dynoed on a chassis dyno with the new engine, and it had about 90kw at the rear wheels.

Second race since all of this work, the engine blew up when oil surge coming onto the front straight at Phillip Island, caused a bearing to spin up, and break a rod. This put a hole in the block, and sump, destroying all but the head, which was untouched luckily. So we rebuilt the bottom end, and bought an expensive Hi Energy sump and modified pickup, in an attempt to avoid costly oil surge blow ups…

The car was much faster now, moving up to mid field, but still too heavy to be a challenger, so it was time for a diet for the car. We put on fibreglass bonnet and boot, and changed the car over from R’s to Slicks. A new triple core radiator was also purchased to fix a problem with the car always running hot, replacing the almost new twin core. For more of a diet, out came the glass windows in favour of perspex and Lexan. The dash and the rear panel was cut out, a new dash pod, fuel tank surround, centre console, steering column support, were all put in. We also removed all unnecessary bolts and brackets, and spent MANY hours removing all body deadening from the whole car, inside, guards, underside, etc, before repainting it. A new seat was installed (lightest and lowest Sparco seat we could afford) and the front left rail was replaced due to the amount of rust the original one contained. A brand new Quaife 4 speed was purchased in from England (A heavy duty straight cut close ratio race box) but we found that not all of the bits were included that we needed. So after a few calls to England late at night, we had shipped out the Quaife alloy casing, and lay shaft to finish the box. A new front spoiler was also installed before the race that weekend at Winton.


At winton with no power

Also that day

The engine was well down on power at Winton, so we checked the compression, but couldn’t find any, so a re-ring was done before the next round. The engine was re-ringed, and re dynoed, this time with smaller chokes, producing more power, 92.9Kw at the rear wheels. We got some 13X8 minilites in silver, making the car look much better. "The Craftsman" Robbie put a centre mount rear wing on the car for us, and a bigger front spoiler. The front ground clearance was reduced to almost nothing…. The front brake pads were finally replaced (the original black flash ones) with Hawk Blues, finally balancing out the braking problems that we had been having since the rear disc conversion. We also put braided lines on all of the flexible hose parts of the brake system.

Finally the car started running well, doing a 1:52 at Phillip Island, and running in second place for a time, until the engine blew up….again…from Oil surge…. Time for the next go…..

So off we went to buy a dry sump system, just intending to dry sump the pinto and put a better bottom end together… Then along came a Cosworth Twin cam 16 Valve head, too good to pass up, and this would all bolt on to what we were doing anyhow. It is about here that things started to get out of hand. now we had a Cossie head, we couldn’t just put rubbish in with it, so off to get the biggest valves that can possibly fit in a Cosworth head, and some big race cams to go with it. We purchased a Cossie turbo crank, a set of Holbay rods and an AP clutch off this guy from NSW, Neville Davis. So we sent the rods and crank off to get machined and prepared. Whilst this was going on, 16 inlet valves arrived from England They had gotten the order wrong, and sent 16 inlets instead of 8 inlet and 8 Exhaust….. Back into the piggy bank for more valves. Then the dry sump that we purchased wouldn’t fit over the rack on the dummy block we were using to test it… We then purchased a brand new Cossie Sierra dry sump pan. This also would not clear the rack, so this one was cut up and modified to fit over the rack. Now we find out that the Crank is cracked and useless, and the rods don’t fit a 2 litre crank, they are for a 1600…. So, furious at the guy Neville from NSW, we asked for a refund on the crank, but he refused to do this, even though the crank was obviously useless. In an attempt to recoup some of our lost money, we sent the crank back to him, and got another for only an extra $500…. this one was ok. The rods had already cost us a great deal being race prepared, so we didn’t let him have them back, not that he would have given us our money back anyhow, let alone more for what we had spent on them. In fact when I complained to him about his latest rip off, he offered to sell us more rubbish….


Cossie on its Dyno runs up to 8500

Very pretty!

Off we went to Argo to get new custom rods. The Holbay rods are an unusual length, and with the custom pistons already finished, we had to stay with that length rod. The head was in the mean time under way when I got another of the standard phone calls… "Jamie I have some bad news….." this time it was only that one of the Camshafts had snapped in half….. In an attempt to make the upcoming race, I rang Bo Seton and got some old cossie blanks from him, made originally for Glenn Seton’s Sierra. Wade copied the cam specs from the broken Ivan Tighe cam to create the new one. We had by this time, of course, decided to fuel inject the engine also, so we went off to see Richard Aubert about getting an Autronic ECU and loom. There was no problem with the ECU, but the looms ended up being a 1 month wait. This caused a few initial problems, but with the rods taking a month, it wasn’t a big deal. Next came the phone call about the head. when the head was returned to be assembled, it was noticed that the cam was wiping off the end of the Volvo shims and buckets. This was another occasion when we had to choose, leave it as it was and hope it would be ok, or take them all out, throw them away, and do it all again properly… and that is what we did… Out with the Volvo buckets and shims and in with the modified Cosworth buckets and Shims.


At Phillip Island just before the end of the engine

The throttle bodies and inlet manifold had arrived, and all was in readiness to assemble the engine. So with a fantastic effort, above and well beyond the call of duty, from Stuey from B&B engine Services, the engine was assembled. We went off, engine in hand, to Dougal McDougal’s (from Victorian Go Kart Centre) brand new DTS engine dyno. Even though this was only a week after Dougals big crash at Phillip Island in the Aloe Vera VS Commodore, everyone there was so very helpful. This made putting the engine on the dyno far easier than expected, and after only a few days for the required fabrication, assembly, wiring, and mounting, we were ready to go.

With A great crowd amassing, the key was turned, and it kicked and sputtered, but nothing. This was of course because I had neglected to load the Ecu with our engine settings. After loading these settings into the ECU, we tried again…. After a short burst on the starter motor to get oil pressure up, it was fired up. Almost 6 months in the making, and the engine began to run…After preliminary checks, it was run in., and checked for leaks. A few small leaks were to be fixed, and we were ready. The rest of the tuning went without much trouble. We were running short of time though, and we had to skip the attempts for max power, leaving cam timing as per the initial specs, and being happy with the 225bhp at 8000rpm on its first run. The fantastic help from Gerry with the Engine dyno, and so much more was great. Richard Auberts assistance with the engine Dyno work was also invaluable and together, the two of them got the most we could possibly get in the time we had.


Dyno Figures from Dougal McDougals Engine dyno in Melbourne (now set up to run both pinto and kent)

Off the dyno, and back to be installed in the car.. This was the Thursday night now, the race being Saturday, we looked like being a good chance to make it, if we went without sleep for 2 day. So with more help from Gerry again, Trevor from TM Automatics, Adam Russell and Kerstin Hahn, we worked through the night putting the engine in. We went ahead, fitting the fuel lines, and fuel pumps, fitting the dry sump, the lines, the covers, the wiring, the radiator, the gearbox, the tails shaft, and the rest of the new bits. This took from about 10pm until 8pm the following night when the engine was fired for the first time in the car. This was an exciting time, but proved to be a bit problematic, as it was first found that the nose of the gearbox was hitting the crank. This problem fixed, we tried again, and all sounded better. The new Willwood callipers were installed in the mean time, ensuring that we could stop when we had to. Kerstin sourced and fitted new stickers, and the whole car polished to look better than it ever had. It went on to the trailer for the drive to Phillip Island.


On the morning of the race also

Off the trailer in the morning we found that we had no drive though the engine and clutch seemed to be working fine. So our with the gearbox to find that the clutch fork was fouling on the back of the bell housing. So with a nip and a tuck on the bell housing, it was all ready to go again. This time it all worked. The spoilers were added, the tyres put on, pressures done, and driven straight to scrutineering, then straight on to the track for race 1. Starting from the rear as we had missed qualifying due to the gearbox problems, the Mk1 took off slowly as a systems check for the first bit of the race. On lap one the car sounded fantastic, and it all seemed to have been worth the effort. On lap 2, the car sounded a bit off beat, and in a familiar sight, we watched the engine explode in a cloud of dollars (smoke) to pull up in the same spot it had the first time….

This was a big bang, only 7000rpm max on the tacho, and the the block had about 5 holes in it that were not meant to be there, including one big enough to put your hand in. To show we are suckers for punishment, we were immediately on the phone, sourcing replacement parts to see try to hurry the return along.

We organised the new parts in no time, actually taking delivery of them is another story. After 5 months, the engine was back together. It wasn’t as easy as you would guess though. On inspection of the top end, thigs were not quite how they should have been. The buckets were wearing very badly, and so was the cam. We found that the valve spring/collet/retainer combination was just plain wrong. The valve springs were all different heights, and pounds at the seat. It seems that the Mini cooper S collets and retainers were not the way to go. They held the retainers about 2 mm too low, causing the valve spring pressures to be way too high, as well as looking like they were coil binding. In all, the work on the head has been a complete disaster. It cost $2000 for the porting and setup of the cams, buckets, retainers and shims. Of this, all but the porting has been replaced or fixed. So time to replace the items, After a long search we found some appropriately sized shims, and some cosworth valve stem seals from S&M Motorsport. Next we found some APE Kawasaki Z900 valve springs, to replace the rubbish that was in it. Then more searching found some more Kawasaki collets that held the retainers exactly 2mm higher than what they were. Finally a setup where everything was where it should be.

In the mean time, another block was sourced, after the original one we got was found to have been cracked down one of the bores already. This new block was well seasoned, found in long grass in a friends back yard, but surprisingly it did polish up quite nicely. The rods finally arrived, well before the pistons which took take far longer to finish than originally expected. A trip to England supplied the new Dry Sump kit (pump, sump, pulleys belts etc) 8 Valves and a Cosworth 4X4 Crankshaft. Of the engine hardware, the only items not replaced were the retainters, the cams and the head itself.

The engine was completed with one week to go before the comback race at Phillip Island. The engine was installed across the weekend, with a small problem being traced back to the clutch plates on the AP twin plate clutch being installed in the wrong order, stopping the bell housing from properly pulling up. By Sunday Afternoon, the engine was ready to be started, so the computer map was installed in the ECU. Whilst preparing for the dyno on the Tuesday, We purchased the Self Mapping software for the Autronic ECU, and the new version of the tuning software. This later proved to be certainly worth the cost, showing us a few little problems before they became bigger problems.


The 50K plate at phillip Island in 1999

The dyno session came and went uneventfully at Bog Cog Offroad in Clayton. The engine was run in, then tuned up to 8500rpm, getting 121Kw at the rear wheels. This compared to the last engine that got 225hp at the flywheel on Dougal McDougals engine dyno. During Sunday of the first event at Phillip Island, the cam cover was removed from the engine to check the clearances on head. This found a new problem for us, with the case hardening chipping off the exhaust camshaft. After much discussion, it was found that the Cosworth buckets are a hard metal, as are the Cosworth Cams, once they have been welded up to build them up from standard. This is causing a problem as the two hard surfaces are causing the cam to come apart.

Where have we gone into the year 2000 with the Mk1?? Well here we are in Mid April, and still waiting for the cams from Tighe Cams. There have been many reasons for this, but all I know is that we have had to pay $200 to repair the cams, which we have wrecked again due to the lateness of the cams. Another $250 for lash caps that we shouldn’t have had to buy, plus another $200 or so to repair the old ones again once the new cams arrive… Most unsatisfactory I do believe. I have also heard from a few others that this cam breaking up stuff is a known problem with this cam and bucket combination, though it does not always happen. It would have been nice to have known this up front.

With help from Defuse Diabates, we have made changes to the car, in the form of new panels, forest arch flares, new paint job, cut from the struts forward off the car and added a new spoiler. We also repaired panhard rod, added an oil cooler, repaired the gearbox, replaced the lay shaft, and added lowering blocks to the rear of the car.

The car was stripped back to bare white by Wayne, a new team member, Kerstin, karl and myself over a few weekends. Below is how it looked when we finally finished removing all the blue stripes from the car, sitting in the painters garage ready to be done.

 

With the paint job completed, it was the beginning of the refitting process. The engine, and the repaired gearbox went in, along with the wiring, and the oil cooler, and the mounting of the spoiler was completed.

 

The car had then to be sent off to get the stickers made, including the numbers, the defuse diabetes logos, the TM Automatics stuff etc. This finally made the car look more how we had intended in the first place.

A rundown of the first few rounds:..............................................................

So off to Sandown for the first round of this year, with a car that was untested, due to waiting for the cams stuffing up our timing for dyno testing and track testing. So we turned up on the Friday, and practiced, finding that the car was overheating, and not sounding quite on song. The overheating was the main problem, so we worked on that all weekend, changing many items across the weekend, trying to bring the temps under control. After qualifying in 6th place, Karl moved up a few spots until Proudfoot decided to turn across the front of the car into turn 3 (causing the broken spoiler shown below with Barry just behind). After stopping to remove the spoiler, Karl dropped back a few spots, only to be worsened by the fact that he was black flagged for speeding in pit lane. So when he came back in again, he decided to DNF as he thought the car was running too hot.

Over the Saturday night, we repaired the spoiler, and tried to fix the overheating problem until late into the evening, eventually getting it looking almost respectable. The second race had Karl starting from the back of the grid, moving quickly through the field up into 4th place, with the car running much better. After passing the MR2 of Ken Hastings, Karl moved into the 3rd place, where he looked destined to stay, until Trevor’s car caught fire down the back straight, and Karl moved into 2nd place. This is where he stayed until the finish of the race 2 laps later. Although most of his race was well done, Karl was able to destroy a few hours work by hitting a witches hat, and bending the spoiler right back to the tyre again. This time it was just race tape to finish the job. In the last race, Karl went straight to the lead, but had to battle overheating, which was causing the rev limit to come down, to a point where the car would not rev over 4000rpm. He battled on to the finish, ending up 4th in the race, and 3rd outright for the weekend. The first real racing trophy we have ever won as a team.

Next it was off to Winton in early April.The Weekend started with the Cams once again not arriving, though we are getting used to this now. So off to the Dyno we went on Wednesday night, just to check that it was running ok. Unfortunately, it was not, the engine was off song a little, and the power was down by 30kw at the rear wheels. It was determined that it may have been a broken valve spring causing this problem, so the head was removed Wednesday night, and taken done to BnB Engine services for checking. Stewy and Joe were, as usual, extremely helpful in getting this done in the rush that it had suddenly become. The car was then moved down to TM Automatics where we did the rest of the preperation work on the car. With an enormous effort from all, the engine was completely checked over mechanically, and given a clean bill of health. This took till about 3am, and we then reassembled the engine. By 5am, the engine was together, and the final work was done. The cars were loaded, and we left as the sun rose at 6am on Friday morning in the pouring rain.

The Friday practice was interrupted by constant rain. with pools of water across the track. During this practice, we determined that the engine problem had not been fixed, but had at least determined that it was not a mechanical engine problem. All that was left was to check the fuel and ignition systems. We found that the fuel pressure was fine when the problem was occurring, so we now assumed that the engine problem was ignition.

Saturday morning, after changing the ignition coil and after checking as much of the ignition system as possible, we started our qualifying session. With a final one lap run, the car did a 1:34.2, to qualify in 3rd place on the grid.

Starting from 3rd place, the car jumped well off the start to be equal second into turn 1, but a slide on turn 1, pushed the car back to 4th place. Unfortunately, the car was deemed to have jumped the start, thanks to a clutch that graps when revved over 7500. So into the pits for a stop go penalty, losing 2 more spots. The escort raced out of the pits to retake 6th place, then 5th place before laps stopped the persuit of 4th and 3rd places....

Race 2 sunday morning left us still with the engine missfire up high, but still able to run the car. This time the start was without incident, keeping the engine revs down till the green light was on, to avoid creeping. Unfortunately, the car was blocked by a poor start from the car in front, and we again dropped down the field. From 6th place, we made our way into 5th quickly, but took some time to pass proudfoot into 4th place. The persuit of the 3rd place car was then on, but we again ran out of laps, ending up 4th.

Race 3 Sunday afternoon left us starting in 4th place. A good start had the escort alongside the leading escort into turn 1, but on the outside, and left to drop back to 3rd when unable to hold the outside line through turn 2. The fast running Trevor McGuiness went passed us into second, when we also moved up into third place. This is how we finished the weekend.

So the result for the weekend for us was great, with an outright third place in the category, and a third place in the 1600-2000cc class.

Ahead of us we have Phillip Island on the 10th and 11th of June, with not too much work to do. The cams need replacing, the engine misfire needs finding and fixing, the front spoiler needs remounting, some diffs need setting up. Also, the front shocks need adjusting, and we need to buy a new race suit each as CAMS have changed race suit regulations, and we all now require new ones

  • Name: Jamie Augustine
  • Birthdate: 28/09/72
  • Birthplace: Melbourne
  • Occupation: Test systems Co-Cordinator (IT)
  • Goals: to win u/2 litre national series
  • Favourite Music: Nrivana
  • Favourite Food: Pizza (is there anything else)
  • Favourite Drink: Scotch
  • First Race: Winton 1995
  • Current Car: Mk1 Escort as above
  • Sponsors: TM Automatics, B&B Engine Services, McDougal Engine Dyno Services, Rowville Exhausts
  • Best Result: Last to 4th in the wet at Winton this year (then crashing whilst leading in the next race)
  • Biggest Thrill: Doing a 1:52 at the island with a carbied pinto....
  • Favourite Story Coming from 4th place in the pouring rain in someone elses car, passing the car owner, then in half a lap, catching and passing into second, then in 2 corners catching and passing the leader, only to slide off into the wall 1 corner later, throwing away the easiest win, and the only chance I have ever had at winning so far....

Here is a photo of the start of the race, then me going into 2nd place in that race.... (Inspired by Ayrton Senna 1993 British GP ??)

Race Diary (Follow the Defuse Diabetes Mk1 Escort's 2000 Season)

 
 

 

Round 1: Sandown

The Defuse Diabetes Escort shows promising form in a positive start to the season.

The week leading up to the race included a night at Moonee Valley at a dinner to show the car, where it looked great, all shiney and new.

Wednesday night, worked till 5am putting engine, gearbox, wiring, plumbing and fuel lines in the car.

Thursday night, started car, loaded it onto the trailer, went down to TM Automatics to finish work on it, put in Gearbox fluid, diff fluid etc. Got home at 3am.

Friday Morning, up at 6am, drive to Sandown, get car ready to race. Do wheel alignment, ride height, fuel car, do tyre pressures, wheel nuts, final checks. -car overheating during the practice, otherwise fine.
-Second Practice, car still getting hot, decide that we need to do something more about it.
-Go to TM Automatics to get bits to insatll a thermostat, and ducting to force air from the brake ducts to in front of the radiator.

Saturday morning.
Slight teething problem with car earth wire causing guages to read inaccurately, disrupt qualifying, still qualify in 6th place.

Race 1, car up from 6th to 4th, when Barry Proudfoot decides to turn in on a corner when there was already a car along side him, and breaks front spoiler off car. Karl pits, we pull front spoiler off car, and he heads back out again. Karl comes in with the car getting hot and we DNF.

Saturday night, the pit crew work till late fixing the spoiler, making almost half of it out of aluminum, by Sunday morning it looks much better.

Sunday
Race 2 for the weekend, the car starts in last, and is in 4th by half way round the track. The car moves into 3rd place by passing Hastings down the back straight. Trevors car retires with a heating problem, and we move into second place. Finish the race in second.

Race 3
Start off the front, and move straight into the lead, leading for the first 2 laps. The car starts to overheat again, and we have to slow. 3 cars pass us before the finish, and we end up 4th. Not the finish we would have liked, but none the less, we are still in a reasonable position in the championship after the first round.

Thanks to all who helped us reach the first round, including Stuart Thomas, Wayne Zaccaria, Kerstin Hahn, Adam Russell, Trevor Mcguiness, Danny Mischok, Danny Pullens and Robbie Pullens amongst many others.

To do for the next round.

Sort out the Overheating problem
Change Camshafts
Dyno Engine for more power
Get spoiler repaired and a spare one made

Round 2: Winton

Round 2 of the Under 2 litre Sports Sedan series saw the first ever Outright and Class podium finish for the Defuse Diabetes Mk1 Escort.

The Weekend started with the Cams once again not arriving, though we are getting used to this now. So off to the Dyno we went on Wednesday night, just to check that it was running ok. Unfortunately, it was not, the engine was off song a little, and the power was down by 30kw at the rear wheels. It was determined that it may have been a broken valve spring causing this problem, so the head was removed wednesday night, and taken doen to BnB Engine services for checking. Stewy and Joe were, as usual, extremely helpful in getting this done in the rush that this had suddenly become. The car was then moved down to TM Automatics where we did the rest of the preperation work on the car. With an enormous effort from all, the engine was completely checked over mechanically, and given a clean bill of health. This took till about 3am, and we then reassembled the engine. By 5am, the engine was together, and the final work was done. The cars were loaded, and we left as the sun rose at 6am on Friday morning in the pouring rain.

The friday practice was interrupted by constant rain. with pools of water across the track. During this practice, we determined that the engine problem had not been fixed, but had at least determined that it was not a mechanical engine problem. All that was left was to check the fuel and ignition systems. We found that the fuel pressure was fine, even when the problem was occurring, so we now assumed that the engine problem was ignition.

Saturday morning, we started qualifying after changing the ignition coil and after checking as much of the ignition system as possible. With a final one lap run, the car did a 1:34.2, to qualify in 3rd place on the grid. Starting from 3rd place, the car jumped well off the start to be equal second into turn 1, but a slide on turn 1, pushed the car back to 4th place. Unfortunately, the car was deemed to have jumped the start, thanks to a clutch that graps when revved over 7500. So into the pits for a stop go penalty, losing 2 more spots. The escort raced out of the pits to retake 6th place, then 5th place before laps stopped the persuit of 4th and 3rd places....

Race 2 sunday morning left us still with the engine missfire up high, but still able to run the car. This time the start was without incident, keeping the engine revs down till the green light was on, to avoid creeping. Unfortunately, the car was blocked by a poor start from the car in front, and we again dropped down the field. From 6th place, we made our way into 5th quickly, but took some time to pass proudfoot into 4th place. The persuit of the 3rd place car was then on, but we again ran out of laps, ending up 4th.

Race 3 Sunday afternoon left us starting in 4th place. A good start had the escort alongside the leading escort into turn 1, but on the outside, and left to drop back to 3rd when unable to hold the outside line through turn 2. The fast running Trevor McGuiness went passed us into second, when we also moved up into third place. This is how we finished the weekend.

So the result for the weekend for us was great, with an outright third place in the category, and a third place in the 1600-2000cc class.

Ahead of us we have Phillip Island on the 10th and 11th of June, with not too much work to do. The cams need replacing, the engnie missfire needs finding and fixing, the front spoiler needs remounting, some diffs need setting up, the front shocks need adjusting, and we need to buy a new race suit each as CAMS have changed race suit regulations, and we all now require new race suits....

Thanks to Stewy and Joe from BnB for their extrodinary help when we really needed it, along with Gerry for his tuning and fixing help, Ian from Bog Cog for his dyno time, Trevor, Scotty, Adam and Kimon for their hours of assistance and advice, Wayne for is invaluable pit work, Kerstin for her assistance, and of course Peter Arnold from Defuse Diabetes for his help to get us here...

Round 3: Phillip Island Raceway (10-11 June)

The Defuse Diabetes Mk1 Escort sports sedan finished on the podium again this weekend at Phillip Island. With 3rd place in class and 3rd place outright from the just completed round #3 of the Victorian 2 litre and under sports sedan series. This places the car in equal second place in the series with four rounds left for this year.

Race week started with the new camshafts arriving from Qld, and being installed by Stwey from BnB Engine services in time for our first dyno session on Wednesday. The missfire that dogged the car throughout the last two races was still there at the dyno, and left us wondering what might be causing it. After replacing the ignition system from the 1 year old MSD to a Bosch HEI, suddenly the missfire was gone... So the mystery was solved... Away we went to purchase our own HEI module, wiring, connectors, and alike. After taking half of Thursday off work, the new ignition system was installed, the dizzy repaired by Gerard Rattigan, and I installed the lot in preparation for the next dyno session. Here the car was checked for full power, which it had, and the fuel mixtures were adjusted.

From here the new hawk brake pads were installed, causing much drama as they seized themselves onto the rotors after only a few medium pace uses on Thursday night. Working right through o remove the pads and rotors to have the checked. Installed the brakes and pads friday morning, retested the brakes, fine this time, fitted new spoiler, did wheel allignment, ride height, camber and caster, loaded the car and tools into the trailer, and off we went.

Qualifying went well with the car running well, beating the cars previous best lap time of 1:51.1 with a 1:50.3. This was still only enough for 4th place on the grid for race 1, but the car was a bit lose in the rear, so more time would come with some changes.

For race 1, we added more rear downforce, evening the cars handling out, seeing the car race up into 2nd place early in the race. The fastest lap time dropped to a 1:48, the fastest lap of the whole race, but still too far back from the leader to challenge

Race 2 was intended to be more of the same, but didnt end up that way. Both Trevor McGuiness and The Defuse Diabetes escort jumped the start with their clutches creeping the cars when they were revved. This earned the two drivers stop/go penalitys, pushing them to last place. From here they raced hard, pushing back through the field, to finally finish in 11th place, a slightly disapointing finish, but better than a DNF.

Race 3 saw the car start 11th, and power quickly into third place, and get stuck behind the MR2 of Ken Hastings. The race was then stopped at half way due to oil down on the track. On the restart, the Defuse Diabetes Escort rocketed into the lead, only to run wide through turn 2 and let Trevor and Ken back through. Only a lap later, and The #55 Escort was trying to pass Ken Hastings when they touched, and Ken went off the track backwards. With only one lap to go, we held second place, to take third place for the weekend.

Another good finish for us, with the car becoming more reliable, and having a pace to match it with the fastest cars in the class. The next round is at Calder Park Raceway on the 5-6th of August. The challenge for us till then is to sort out the creeping problem evident during race starts, and of course, search for more power... you can never have too much power...

Round 4: Calder Park Raceway (5-6 Aug)

Another Solid 3rd place for the Defuse Diabetes Mk1 Escort.

After problems withe jumping the start over the last few rounds of the series, we have been making a few changes to the car to ensure clean getaways. This along with changes to the fuel lines, axles, and battery location have been the total of the changes made to the Escort between rounds 3 and 4 of the series. Reliability rather than more speed has been the emphasis, and seems to be getting us at least reliable, if not gaining us race wins.

Friday 4th of August

Private practice on Friday the 4th of August gave us clear skys and good weather. An excellent chance to test where we were in terms of speed compared to others in the championships. The Under 2 litre Sports Sedan lap record was 1:04.37, but we had not been here for a few years so didnt know what to expect. We started doing times of 1:06, but got down to 1:04.7 by the end of the day, only .4 off the lap record. Over the day we had an Exhaust break and bounce down the road (due to a broken locator tab) and a starter motor give up working. Both quickly fixed.

Saturday 5th of August

Qualifying started with us getting stuck in traffic, giving us plently of slow times. Finally a few clear laps saw us get a 1:04.3, equalling the lap record. A slight problem during qualifying was a dogy stopwatch, showing times about 3 seconds slower than the actual times. So the lap board was showing 1:07 when the laptimes were 1:04. this problem aside, we ended up qualifying in third place, with the front 2 cars running times in the 1:03's, under the lap record by a second.

Race 1 Saw us go from 3rd on the grid to almost last, as I almost stalled the car on take off from the line. From here we pushed back past the traffic as fast as possible, making it back up to third place with 1 lap to go. On the last lap, whilst slowing down with no one behind me able to catch up, The lead car came back upon us. He had been in for a stop/go penalty for jumping the start, and was coming back through the field. I was able to just hold him off to take third place in the race, a good comeback considering how poor the start to the race
was.

Sunday 6th of August.

Race 2 meant starting from 3rd place and was an enthralling battle for the lead. Peter Elvey took off into the lead, with Trevor in second, with me in third, and Luke Mcpherson off a bit in fourth. The first few laps saw me pass trevor into second, then push Peter around the lap till all 4 of us came into turn 1 together. In a high speed braking duel, Elver repassed Trevor, whist I ranged up alongside them. Then from behind came Luke who dived up the inside of me, leaving the Diabetes Escort pushed back to 4th place. From here I battled to find a way passed Elvey into 3rd, but ran out of laps to finish 4th.

Race 3 we started from fourth, and with a good start, jumped straight into third place. From here I battled with luke for the first lap until something went bang in the rear of the car under brakes behind Luke. I slowed, trying to determine what the noise was, letting the field behind catch back up. With the noise going
away, I sped back up, just enough to hold the rest of the field back, and maintain 3rd place for the rest of the race.

A third place outright, and third in class for the Defuse Diabetes Escort was a strong outcome, leaving us well in the hunt for this uears championship. The current pointscore is as follows

Luke McPherson 204
Diabetes Escort 55 200
Trevor McGuinness 200
Mark allan 174

For next round, a new Exhaust is in order, and an investigation into the noise from the last race.

 

 

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